• Cabinet Reminders:
    • Connect Award
    • Schedule team-wide HOLA syllabi meeting
  • Announcements:
    • Next Scrimmage: 11/15 Hawkins High School (7:30 AM - 1:00 PM)
    • Weekly assignments on Schoology are now a part of weekly check-ins
    • HOLA Meeting discussion
  • Team Outline

  • Team Duties:
    • Artemis:
      • Discuss Timeline for V2
        • Either Auton or Driver Practice
        • Attach Poly Carb
    • Apollo:
      • Discuss timeline for V2 Robot
        • Turret Pros:
          • +1 degree of freedom
          • Very compatible with limelight (especially during autonomous)
      • Fix minor issues Max posted:
        • Drive motor loose: I forgot which drive motor is loose, but one of the motors on the drive train is not fully connected to the L-gear box and starts turning back and forth when the robot moves. You guys will know what I'm talking about if you drive the robot around and look at the motors.,
        • Fitting 3 Balls: Try to move the shooter farther up the ramp by reducing the spacers. It should be pretty simple; it's super close, just do what you think is best. Then try practicing shooting with three balls.,
        • Straighten Shafts: I know straightening the shafts is hard, and I don't know how much it does, but we should try tomorrow, and we don't have new ones yet. In terms of getting new ones, I made sure to add them to the ELOP funding list a month or two ago, and if I'm correct, they should arrive sometime in November. If not, I will just order them via Robotic's bank account (Hackclub).,
        • Other little tune-ups: I think it’s best to go through and tighten everything tomorrow, make sure supports are perfectly straight, etc. I think I also noticed a small crack in one of the 3D prints for the drive. If you guys see this, let me know, and I can reprint it on Tuesday.